Subject: re : basin production from ga 213 daren , i ' ve just received word from basin to bring production on sometime today or tomorrow ( they expect to get up to b / t 10 , 000 - 15 , 000 d ) ; if our facility planning engineer determines that we can take the gas , then it will flow for all of february and be priced at 100 % gas daily less $ 0 . 16 . vlt daren j farmer 01 / 25 / 2001 01 : 47 pm to : vance l taylor / hou / ect @ ect cc : subject : re : basin production from ga 213 i need for you , or the producer services group , to determine if you think the gas will flow for the month and at what price . i will use your decision for our bidweek postion . d vance l taylor 01 / 25 / 2001 11 : 53 am to : daren j farmer / hou / ect @ ect , robert cotten / hou / ect @ ect cc : susan smith / hou / ect @ ect , melissa graves / hou / ect @ ect subject : basin production from ga 213 fyi , how would you want to handle for february nomination ? vlt x 3 - 6353 - - - - - - - - - - - - - - - - - - - - - - forwarded by vance l taylor / hou / ect on 01 / 25 / 2001 11 : 55 am - - - - - - - - - - - - - - - - - - - - - - - - - - - enron north america corp . from : brad blevins 01 / 25 / 2001 10 : 56 am to : john peyton / hou / ect @ ect cc : nick cocavessis / corp / enron @ enron , steve - hpl - schneider / hou / ect @ ect , pat flavin / gco / enron @ enron , vance l taylor / hou / ect @ ect , buck thomas / gco / enron @ enron subject : basin production from ga 213 i have reviewed the gas composition analysis from spl of the basin production from ga 213 . while spl ' s analysis does show a dewpoint of around 20 degrees f at 400 psig , it is both my and john handley ' s opinion that the gas from the wellbore had stratified by the time that this sample was taken . we expect the dewpoint of the flowing gas to be higher . however , this was the best sample that could be obtained at the time . we have conferred with steve schneider and we are willing to take this gas on a conditional basis over the next couple of days . once the 6 " line has been pigged , the production flows stablilized and mitchell ' s conditioning equipment lined out over the next couple of days , hms will need to take another sample at the meter run and have spl run an extended analysis with a dewpoint curve on an expedited basis . should this sample indicate a dewpoint over 45 degrees f , then this production will be shut in again until hydrocarbon dewpoint conditioning equipment has been installed . in the meantime , hms needs to keep a close watch on all southern union city gates on galveston island to monitor for liquids fallout .