Subject: re : shut - in of # 986315 fyi - we don ' t have any active contracts behind this meter . there was a dedicated reserves purchase contract with phoenix gas pipeline company that terminated 7 / 31 / 99 . there was also a gtc - lst purchaser / marketer with el sordo gathering systems , inc . which expired 8 / 1 / 99 . if you are aware of any other contract that we don ' t reflect in the global contracts database , please let me know . otherwise , there isn ' t any action that my group needs to take regarding this shut - in . enron north america corp . from : gary a hanks 06 / 15 / 2000 11 : 18 am to : cheryl dudley / hou / ect @ ect , pat clynes / corp / enron @ enron , daren j farmer / hou / ect @ ect , shawna flynn / hou / ect @ ect , james mckay / hou / ect @ ect cc : subject : shut - in of # 986315 meter 0986315 shawnee spring common point was shut - in on 6 / 13 / 2000 due to high dew point . repeated attempts by the pumper to dry out the gas have failed . the meter will remain shut - in until the dew point is within pipeline quality specs . gary h . - - - - - - - - - - - - - - - - - - - - - - forwarded by gary a hanks / hou / ect on 06 / 15 / 2000 10 : 47 am - - - - - - - - - - - - - - - - - - - - - - - - - - - from : sean j smith 06 / 14 / 2000 05 : 55 pm to : gary a hanks / hou / ect @ ect cc : subject : # 986315 i received a call from carl drachenberg with hms at approximately 1 : 45 pm on 6 / 13 / 00 stating that he pulled a stick on meter # 986315 and it was wet and flowing at 35 lb . i asked gary hanks what we want to do and he said to have carl notify the producer and shut it in . i notified carl and he got in touch with the producer and they shut the compressor down at approx . 2 pm on 6 / 13 and at that time there wasn ' t any flow . carl came back out there at 8 am on 6 / 14 and closed the valve and removed the chart . there was no flow after they shut the unit down and it was flowing between 500 and 300 mcf . the meter is now out of service . any questions - you know where to find me .